Yes it is. I have been busy.
Wednesday AM we arrived at the boat about 8:30. Scott, the Mechanic, was scheduled for 9AM. Got to the boat about 9:30. After surveying the problem Les and I went about setting up the A-frame Bases while the Mechanic went to his shop to get additional blocks of wood to serve as braces.
My boat has a cockpit port over the engine, where the control gauge panel sits. I removed the panel and the port cover. From there we dropped a come-along into space above the engine. This allowed us to vertically lift the engine off the motor mounts.
The mounting brackets were too wide to fit through the bulkhead opening, so I removed them while Les and Scott supported on blocks a 4x4 above the companionway. Attached a come-along to the engine and pulled the engine through the bulkhead while easing the hold through the port. The engine swung gently into the cabin. Once in the cabin, we set the engine down on a pair of 2x4's and rearanged the A-frame to get the engine up and out to the cockpit. From the A-frame in the cockpit Scott positioned an aluminum I-beam to over the engine on a 4x4 across the companionway. Again center lift out of the cabin. This time the come-along pulled the cable loop that was over the over the I-beam along into the cockpit. One last set down and reset of the A-frame. One A-frame in the cockpit and one A-frame on the dock. It was a stretch but the system worked with the boat snug up tight against the dock, we made one final lift and moved the 400lb block to the dock. Did not dump the engine block into the water.
The rig looked something like this. There were no wheels. The unit made from aluminum was managable on the boat.
Even though the fluids had been drained there was a little residual left in the engine and hose outlets to make a bit of a mess. Shop towels, some cleaner and most of the spots are gone. With the new empty space over the bilge, I will finally be able to clean up the black hole.
Scott took the engine to his shop and started the process to dislodge the pistons from the block. Here are the images I received Thursday afternoon.
He said cylinders 2 & 4 had a lot of rust. The pistons were frozen in the block. No apparent damage to the block crankshaft or bearings. All still need to be inspected. Unclear where the water entered the block. That is under investigation. He thinks a rebuild is possible. Is putting together a list of parts and will contact me with the news - a quote.
I remain hopeful.
At the present repair of SV Hadley seems more likely than 3 weeks ago.