How To: Replace engine mounts, damper plate, and transmission on a Catalina 310.

Jul 28, 2024
41
Catalina 25 Portland, OR
Background:

My 2003 Catalina 310 had the standard Universal M25XPB with Hurth 50 a.k.a. ZF HBW50 transmission with around 900 hours. The setup never let me down in the past 1.5 year that I've owned the boat, but I did have two concerns: 1) Plenty of posts on this forum and others reported failures of Hurth 50's around 800-1000 hours, and worse yet that rebuilds seemed to universally fail, and 2) very prominent engine vibrations and "chattering" sounds at idle.

After lots of research and planning, I actually talked myself into replacing the damper and motor mounts and upgrading to a Twin Disc transmission all at once. The more projects I do, the more I realize that if I assign a modest labor rate to my own time, it's usually both worthwhile and rewarding to replace everything that wears out "while you're in there."

After replacing all three things and re-aligning the engine, the boat has dramatically less vibration and chatter. It's still not perfect, and I suspect with a 3-cylinder never will be, but I'm very happy with the improvement. I no longer find myself fidgeting with engine speed to find a cruising rpm that doesn't cause the hatches to rattle, and idling down from cruising speeds to idle RPMs no longer produces sounds like bolts rattling around in tin cans.

I'm now very happy to listen to the motor at 1100 RPM idle speed (which I adjusted according to the Universal bulletin), whereas before I found the rattles deeply displeasing. I'm happy to know I'm running a brand-new transmission with a far superior reliability reputation to the one it replaced.

The only downside is that the Twin Disc TMC-40 transmission uses straight-cut gears, whereas was the Hurth/ZF boxes, along with the ones fit to Yanmars, all use helical cut gears. Straight-cut gears produce a higher-pitched whine sound that changes with gear speed. The folks at Beta Marine confirmed this is normal, as did other threads from folks who made the same upgrade. In the fullness of time, I plan to install some more sound proofing in the transmission tunnel area to quiet this down. While a little annoying, I'm still happier to take a slight increase in mid-frequency sound over all of the rattling and chattering that was eliminated. If you don't know what straight-cut gears sound like, they are often used in race car transmissions and rear-ends. This is a great example of the sound: Straight Cut Gears Sound Amazing. Don't worry, the transmission isn't actually that loud, but the sound and the linear relationship of pitch to engine speed is similar.

Research and parts selection process:

After much research I discovered the "chattering" sound is often liked to a failed damper plate, and found many success stories on the C350 forums of folks replacing the plate with an upgraded model and enjoying reduced vibrations. I found this post particularly helpful: ENGINE NOISE-DAMPER REPLACEMENT? - Catalina 350 International Association. This thread and others point to there being two versions of the rubber-based "R&D" brand damper plate used - a "standard" model from the factory and an "H/D" model is later upgrades. I posted a follow-up below about the differences in these models.

R&D damper plates are distributed in the US by PYI Inc, and I called and spoke to a very helpful gentleman at PYI who confirmed the "H/D" model was a much better choice for our engines. The "standard" model damper was not well suited to absorb all the torrential vibration from the Kubota 3-cylinder block of the Universal engine which, compared to other engines such as Yanmar, has a relativity lightweight flywheel. While I didn't know for sure during the planning phase if I had my original damper plate, if a prior owner replaced, if it was the upgraded model, or what it's condition was, my complaint of chatter seemed to align with needing a damper replacement.

I ordered part # RD-22-AM-4 from PYI for around $400 - this is the "H/D" (High Deflection) version of the damper, while the standard "Loop" version shipped by Universal on the engine originally would have been # RD-22-A-4. This catalog has a breakdown of the part numbers: https://www.pyiinc.com/downloads/r-d-marine/r-d-marine-catalog.pdf. See the follow-up post below for more info.

There also seems to be some debate about abandoning R&D dampers altogether and moving to a more traditional spring-based damper. Catalina Direct currently sells a spring-based damper for $1219. I've read about issues with spring-based dampers as well, so decided to stick with the much cheaper RD-22-AM-4 based on what I had read about successful service life after replacement.

Threads about vibration and chatter will almost always recommend replacing engine mounts. I had the original Universal-style mounts (see photos below) which looked fine, but I had no real way to tell their condition. I did notice that at certain engine RPMs, the prop shaft was hitting the log and causing rattling to spread throughout the boat. I could reproduce this even in neutral and pause it by simply grabbing hold of the shaft and manually absorbing some of the wiggle being produced by the engine. I figured this could probably be solved by adjusting the engine position via the engine mount adjusters so the shaft was better center in the long, but since I was already going to have to lift the engine to remove the transmission so I could access the damper plate, starting fresh with new mounts before alignment seemed logical.

The Universal mounts are expensive. The OEM Universal part # is 040510. Westerbeke sells them right now for $659 each, and Catalina Direct sells them for the same. I was tempted to move to a much cheaper aftermarket mount, but two things deterred me: 1) this thread which highly favors the Westerbeke style: Anyone Tried These Motor Mounts and 2) the mounting pattern. The Westerbeke mount holes to the boat are 5" on center, whereas all the aftermarket mounts I found were 4". I had no interest in adding the drilling of new holes and filling of old holes into the labor of the project, so I bit the bullet and ordered 4x 040510's which were mercifully only $421 each when I ordered them a few months ago.

After spending about $2,000 on the damper plate and mounts, I got busy with other things for a while. When I got back around to the project a few months later, and with a dear friend signed up to spend the day on the installation with me, I started thinking about how silly it would be to spend all those labor hours to reinstall that Hurth transmission, known to fail, when a well-respected replacement was available for about $1,200. The old transmission literally has to be fully removed in order to access the damper plate, so since I was this far in, why the hell not replace the transmission while I was at it?

The Hurth 50 - which later became the ZF 5M when ZF bought Hurth, is no longer made. The next size up replacement from ZF is the ZF 10M, which Catalina direct reports as being hard and expensive to get and recommends the ZF 12M instead: Transmission - New Replacement 12M. The problem is that the 12M is 1.46" longer and has a 0.39" bigger drop (from input shaft to output shaft) than the original Hurth 50. That 1.46" length increase would be very involved to accommodate, as there's less shaft than that exposed between the dripless seal and the flange. At the very least, new holes would have to be drilled to push the mounts forward, and the engine cover would probably have to move forward as well requiring some trim on the bulkhead to accommodate the gap, maybe the shaft shortened. Yuck. The Twin Disc TMC 40 is a far closer match, being just 0.157" longer and having 0.216" more drop. Beta Marine sells it for $1260 (TMC 40 (2:1 ratio) Transmission) and supplied this very helpful document about the considerations when converting: CONVERSION FROM ZF 5M (HURTH HBW 50) TO TMC 40.pdf. I ordered the transmission from Beta Marine, along with the horizontal control cable bracket (part# 202-09311), bracket hardware (2x #217-99292 and 2x #217-99293) and saddle clamp fitting (part# 212-99241/01) all for $1252.39 including shipping with their new user online discount.

Reading a post from Jesse's blog (Engine), and others in the 310 forums, it seemed folks liked to install spacers below the motor mounts so the engine doesn't sit up so high on the mount bolts. Perhaps this helps reduce vibration by giving the engine less leverage to flex the rubber. Since I was already at least half way up the bolts, and was going to need to raise 0.216" to accommodate the bigger transmission, I decided to make some mounts. I've worked with a local shop that can laser cut parts out of stainless steel up to 3/4" thick (which is nuts), so I designed my spacers in CAD, 3D printed to test fit, and then had the shop (Profile Laser in Portland, OR) make 2x spacers out of 1/4" 304 stainless for the back and 2x out of of 1/2" stainless for the front. Here's the drawing for my spacers as PDF: DENTON-ENGINE-SPACERS-V02-NOV-02-2025.pdf. I'm happy to provide a DXF version via email if you'd like to get some of these made. Profile Laser cut my four spacer, plus an extra part for my bowsprit project, for $250.

The spacers are very pleasing hardware:
Spacers.jpeg


In the interest of being over-prepared so my generous friend and I could complete the project in one day, I also ordered new hardware:

Bolts for mounting plate to transmission:
> 6x M8, standard 1.25 thread, 20mm long, class 10.9 steel, plus lock washers

Bolts for holding mounting plate to engine block:
> 6x M10, standard 1.5 thread, 25mm long, class 10.9 steel, plus lock washers

Bolts prop shaft flange to transmission:
> 4x M10, fine 1.25 thread, 30mm long, class 10.9 steel, plus lock washers and standard nuts

I used regular zinc fasteners, based on recommendations I found against stainless for this application due to galling risk. I confirmed Beta Marine uses non-stainless fasteners for such applications as well.

I bought blue LocTite for the transmission mounting bolts.

The damper plate attaches to the flywheel with special Allen-socket style screws that use a 4.5mm Allen key. Since these were so specific I ordered them from Westerbeke, 6x part # 200443 @ $3.50/ea. They come with LocTite red pre-applied, which makes sense given their important job and small size, but sure made the old ones annoying to get out.

I also ordered the replacement gasket that goes between the exhaust manifold and the mixing elbow, because it was easiest to remove the mixing elbow and disconnect the hose from the muffler than to try and remove the hose from the elbow. The gasket is part # 036425 from Westerbeke.

The project requires lifting the engine a few inches to get the new mounts in. I didn't like the idea of lifting via the boom, so I purchased 1x 8' 4x4 lumber and chopped it into three pieces. Two of the pieces I wrapped in felt to set on either side of the companion way without scratching, and the third piece to set onto as a cross-bar. I bought a very cheap chain hoist from Harbor Freight to hang from the rig. We found that while it lifted fine, the transition to lowering was sketchy and at one point dropped the engine about an inch before engaging. I returned it and would recommend a better quality chain hoist.

In addition to standard tools, I also brought the following which all turned out to be super helpful:

* An electric 3/8" drive ratchet - great for the very long threaded bolts that hold the motor mounts to the boat
* A bunch of long 3/8" drive socket extenders, allowed using the electric ratchet from the top when working on the mount books
* A set of standard and "stubby" metric ratcheting wrenches - these things always make life better
* A good set of feeler gauges for the alignment
* Torque wrenches, although there don't seem to be rigorous torque specs for any of the bolts involved

Armed with hours of research and every part and tool I could think of, we went to the boat.

In the following posts I'll show the pictures through the process. The two of us were able to complete the project in about 7 hours.

Yes, I know this post was a mile long. I hope it helps someone who takes on this project next!
 

Attachments

Last edited:
Jul 28, 2024
41
Catalina 25 Portland, OR
Installation Process:

1) Removed the top nut and mounting bolts from all four motor mounts. The top nut is 13/16" A friend with the same motor loaned us a 13/16" offset wrench that helped getting to the port-aft nut. The other three were easy with a standard socket. The mounts are held to the boat with threaded bolts into a tapped backer plate. I thought they would be standard lags, but it seems Catalina nicely installed backer plates instead. These bolts had 9/16" heads, and must have been fine thread as they took a lot of turns to get out. 6 of the 8 total bolts could be removed from the top with 2x 1' drive extensions and the electric ratchet, which was a dream. 2 are hidden under flanges of the engine and required a ratcheting wrench to remove.

2) Removed the bolts coupling the prop shaft to the transmission output flange.

3) Removed the exhaust elbow from the engine, and pulled the exhaust hose off of the muffler. At this point the exhaust hose and elbow together could be lifted out from the front and set aside.
Exhaust_Hose_Out.jpeg


4) Pushed/pulled the engine about 2" forward. This took a bit of a shove but was pretty easy. Thankfully, all of the other hoses accommodated the 2" of movement.

5) Set up our hoisting rig on top of the companionway:
Hoisting_Rig.jpeg


6) Hosited the engine, by its built-in lifting point, about 3", keeping a close eye on all the hoses and wires. The goal was to lift enough that the back of the transmission had completely cleared the prop shaft flange, so the transmission could be pulled off:
Lifting.jpeg


7) Removed the negative ground wires from the engine, as these were the tightest appendage when lifting. We were surprised by a spark, because it turns out the negative for the entire battery bank runs through here, so our house loads were running through. We turned off the battery switch and temporarily bolted them together so we had house power for our lights:
Ground_Wires.jpeg


Ground_Wires_Bolting.jpeg


8) Removed the 6 bolts that hold the transmission mounting plate to the back of the motor (10mm bolts, 17mm wrench). Most were accessible with the long driver extender from the rear, a couple required wrenches from the side:
Mount_Bolt_Side.jpeg


9) Disconnected the shift linkage cable from the transmission.

10) With some wiggling and manual pulling, the transmission and it's mounting plate pulled off the back of the engine and could be lifted free:
Removal.jpeg


11) Removed the 6 bolts that hold the mounting plate to the transmission.

12) Moved the mounting plate to the new transmission, the bolt holes lined up perfectly. We used 6x new 8mm bolts, lock nuts, and LocTite blue, torqued to 22 ft-lbs.

13) Wished at this point we had pre-installed the 6x bolts + lock nuts that hold the mounting plate to the engine block into their holes in the mounting plate. Once the transmission/plate are seated on the engine, one of the bolts is very difficult to get into the hole.

14) Removed the old damper plate. It's held in with 5 Allen-head screws that use a 4.5MM key. Not 4mm, not 5mm, 4.5mm. The one size I didn't have in my fancy ratchet-drive set. I used a regular Allen wrench with a nut driver slid on the handle for extra torque. The old bolts were in tight and with LocTite red, so they require force all the way out. Once removed, it looked like the damper might have been replaced already, but it was the "Loop" style not the recommended "High Deflection" style - see follow-up post below.
Old_Damper.jpeg


15) I did notice that the input shaft on the transmission was a bit chewed up and fit a little loose on the old damper plate, so perhaps that was in fact the source of the rattle. Inside the flywheel of the engine, there was a ton of brown dust. Perhaps from the demise of the original damper? I cleaned the dust out as best I could:
Flywheel.jpeg
 
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Jul 28, 2024
41
Catalina 25 Portland, OR
16) Installed the new RD-22-A-4 damper, using new screws from Westerbeke part # 200443. I couldn't find a torque spec for these, and I couldn't use my torque wrench anyway since they were the odd 4.5mm size. I tightened the new screws, which came with LocTite red pre-applied, as tight as a I could with a standard Allen wrench and a nut driver applied as a lever for extra torque. I tightened in a several-stage star patten, like tightening lug nuts.

17) Greased the input shaft of the transmission with some grease. Beta marine didn't think the type of grease was particularly important, I used Quicksilver 2-4-C.

18) Set the new transmission into place, slid the shaft into the engine, and seated the mounting plate on to the pegs that stick out the engine block to align it:
Trans_Going_In.jpeg


Trans_Going_In_2.jpeg


19) Installed 6x new 10mm x 25mm standard thread pitch bolts with lock nuts and LocTite blue, torqued to 50 ft-lbs. We tightened gradually to make sure the transmission set square to the engine as it was tightened.

20) Removed the old motor mounts, which required only lifting that corner of the engine by hand to adjust the balance as it hung from the hoist chain.

21) Installed the new mounts, using the 1/2" spacers in the front and 1/4" spacers in the rear.

22) Lowered the engine onto the new mounts and spacers and removed the hoist.

23) Slid the engine back to where the transmission output flange and propshft coupling almost met.

24) Adjusted engine height on the mounts until the transmission output flange lined up with the prop shaft while I held the prop shaft in what I guessed was the center of the log.

25) Pushed the engine all the way back, seating the transmission output flange to the prop shaft coupler. To accommodate the extra 0.157" length of the new transmission, the prop shaft was pushed slightly out of the boat and the billows of the PSS shaft seal was compressed an extra 0.157". The billows compression could have been eliminated by sliding the sealing ring forward 0.157" on the shaft, but since the billows is already compressed around 1" from it's neutral position, it seemed fine to compress it a little more.

26) With the engine back over the old motor mount bolt holes, we installed the new mount bolts, leaving them loose until we checked alignment:

New_Mounts.jpeg


New_Mounts_2.jpeg
 
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Jul 28, 2024
41
Catalina 25 Portland, OR
27) Using feeler gauges, we made minor adjustments to the engine port-aft position until the gap on the port and aft sides between the transmission output flange and the prop shaft flange was a close as we could get it. With every adjustment, we rotated the shaft by hand a couple types before measuring again. When we started, the difference was maybe 10 thousandths. With gentle taps with a hammer on the corresponding motor mounts, we got down to 1 to 2 thousandths of difference between the port and aft side measurements. We locked down the motor mount bolts to the floor and confirm nothing moved. This was a very satisfying process.

28) Dialing in the alignment between top-vs-bottom gaps on the flanges was even easier since the front of the engine could be raised/lowered precisely with the lock nuts on the motor mounts.

29) Tightened the bolts between the transmission output shaft flange and prop shaft coupler:
Output_Shaft.jpeg


30) Re-installed the exhaust elbow and re-connected to muffler. Getting the exhaust elbow aligned with the output flange on the manifold and then getting the v-ring clamp on, while fighting with the pressure of the hose, is unpleasant but doable.

31) Installed the shift linkage cable to the bracket and adjusted linkage so shift lever was centered in neutral. It turns out, the direction control on the Twin Disc is opposite that of the Hurth. We were very surprised to find out the shifting lever now operated backwards.
Linkage.jpeg


Beta Marine sent me the following picture of how the linkage can be adjusted to correct the direction of the lever:
Linkage_Reversal.png


As the time of writing, I haven't yet made the change to the linkage as shown above, but it seems like it should work.

32) Filled the transmission with 400ml (0.4 L) of Dexron 3 ATF.
 
Last edited:
Jul 28, 2024
41
Catalina 25 Portland, OR
After writing this up last night, I got curious about the difference in the damper plate that was recommended by PYI vs the one I removed.

On page 16 of the R&D marine catalog from PYI (https://www.pyiinc.com/downloads/r-d-marine/r-d-marine-catalog.pdf), there this handy picture and description of the different damper element types:
Element_Types.png


The type that I removed is the "Loop Type," which is what I believe Universal shipped our engines with, code "A" in the part #. The type recommended by PYI and on the C350 forums in the "High Deflection" type, code "AM":
Element_Table.png



It looks like the OEM "Loop" type only allows for 3 degrees of flex, where the "H/D" allows for 30 degrees. That could explain a lot. Our little three-cylinder engines with light flywheel are going to have a lot of torsional jitter at low RPMs, and the loop type is only going to eat up a few degrees of that before passing it along to the input shaft of the transmission – which will both create rattles and wear the transmission. Seems like the H/D is going to pick up a lot more of that slop with its 30 degrees of deflection.
 

jssailem

SBO Weather and Forecasting Forum Jim & John
Oct 22, 2014
23,769
CAL 35 Cruiser #21 moored EVERETT WA
An intensive refit. I suspect you will enjoy the results and any costs will soon be forgotten. Your boat and crew will appreciate you for the successful project.:biggrin:
 
Sep 24, 2018
3,913
Catalina 30 MKIII Chicago
This is an amazing amount of detail you've put into this! This will surely help many people for years to come. I wish service manuals had half as much detail!
 
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