A
Andrew Flood
I recently installed an Autohelm 4000 wheelpilot. The install went smooth as well as the calibration, but I am having a problem maintaining a steady course when under engine power with the RPM greater than 2500. If I motor less than 2500 it is rock steady.It will deviate back and force by 45 degrees and never settle down to a stable heading when greater than 2500 RPM. Is this prop wash causing this or is the autopilot at fault? I have this installed on a 1989 H30. Any comments appreciated.